无压隧洞洞内消能试验研究  被引量:16

The experimental research of energy dissipation in free-flow tunnel

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作  者:邱秀云[1] 侯杰[1] 王锟 

机构地区:[1]新疆农业大学水利与土木工程学院,乌鲁木齐830052 [2]伊犁州水利水电勘测设计院,伊宁835000

出  处:《新疆农业大学学报》2004年第3期62-65,共4页Journal of Xinjiang Agricultural University

基  金:新疆水利水电工程重点学科基金项目资助

摘  要: 通过新疆喀什河吉林台一级水电站引水隧洞水力学模型试验,对深孔式无压隧洞洞内消能及消能工型式进行试验研究的成果,提出了在无压隧洞洞内设置消力池加悬栅的消能工型式。试验表明,悬栅的置入增大了掺气量,并且起到了破碎水跃表面波浪的作用,从而削弱了因池中水波而引发的下游洞内涌浪。该消能工的消能率达90%以上。The energy dissipation and the form of dissipater in deep hole free flow channel are studied in this paper through the hydraulic model experiment of diversion tunnel in Jilintai first-order hydropower station, which is located on Kashi river, Xinjiang. This paper reaches the new form of energy dissipater in free flow channel named suspended grid dissipater. The experiment indicates that aeration degree increased after putting suspended grid dissipater, and it also breaks the surface wave of hydraulic jump which can cause the surge in downstream. The computational results show that the damping ratio of such dissipater can be above 90%.

关 键 词:无压隧洞 消能 试验研究 

分 类 号:TV651.3[水利工程—水利水电工程]

 

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