官69断块微生物驱油现场试验效果分析  被引量:11

Microbial flooding in Guan 69 Block, Dagang Oilfield

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作  者:王学立[1] 陈智宇[1] 李晓良[1] 路永萍[1] 张仕明[1] 李秀兰[1] 倪金忠[1] 段冠青[1] 

机构地区:[1]中国石油大港油田南部油气开发公司

出  处:《石油勘探与开发》2005年第2期107-109,共3页Petroleum Exploration and Development

摘  要:针对大港油田官69断块油藏高含水期水驱效果差的情况,在4个井组实施微生物驱油试验。在断块4 口注水井中注入相同用量的菌种(前缘段塞用胶结能力强的菌种DG002和N80,主体与后尾段塞用N80)后,2 个井组见到较好效果,产量递减放慢、开采状况基本稳定,或者产量增加,含水下降。受益井官69 8井日产从21.88t上升到23.3t,官69 21井含水从95.6%降至93.7%,减缓了区块产量递减。With water cut rising up, the effect of water flooding on the recovery of the Guan 69 fault-block in Dagang Oilfield became worse. The same amount of microbaterial seeds is injected in each of the 4 injection wells. The DG002 and N80 with special effect on gel is used in the front plug, the N80 is applied in the main and the final plug. Two of the 4 testing well groups got better effects with slower yield decline and stable production performance. The yield of guan 69-8 is up to 23.3 t/d from original 21.88 t/d and the water cut of the Guan 69-21 decrease to 93.7% from original 95.6%.

关 键 词:高含水油藏 微生物驱 现场试验 效果 

分 类 号:TE357.4[石油与天然气工程—油气田开发工程]

 

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