改良序批式活性污泥法处理校园污水的试验研究  

Research on Treatment of Campus Sewage by Modified Sequencing Batch Reactor System

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作  者:安长伟[1] 张显龙[1] 王丽多[1] 

机构地区:[1]沈阳化工学院,辽宁沈阳110142

出  处:《当代化工》2008年第5期522-525,558,共5页Contemporary Chemical Industry

摘  要:SBR法以其运行方式灵活的特点可以实现对不同污染物去除的控制。试验基于此特点,通过改变SBR工艺的运行方式,考察不同运行条件下CODCr、NH3-N、TP的去除率,从中确定最佳运行参数。在进水搅拌45min,进气量0.5m3/h,曝气5h,停曝搅拌75min,沉淀75min的最佳运行参数下,稳定运行8个周期,进水CODCr、NH3-N、TP的平均质量浓度分别为353.8mg/L、33.70mg/L、0.714mg/L时,出水CODCr、NH3-N、TP的平均质量浓度分别达到30.26、9.322、0.458mg/L。SBR process can be achieved for different pollutant removal by controlling. Based on this characteristics the feature compared the removal rate of CODCr NH3-N,TP under different operating conditions using a changed mode of SBR operation, then ascertaining the optimum operating parameters. The optimum operating parameters gained is as follow:the mixing time is 45min during the falling in of wastewater, the feed rate is 0.5m3/h, aeration time is 5h,aeration after mixing time is 75 min, sedimentation time is 75 min,and then operated stably for eight cycles,the he average quality concentration of the CODCr NH3-N,t TP in the influent were 353.8mg/L,33.70 mg/L, 0.714 mg/L respectively, and the average concentration of CODCr NH3-N,TP in the effluent were 30.26mg/L, 9.322 mg/L,0.458 mg/L respectively.

关 键 词:SBR 脱氮除磷 运行方式 最佳运行参数 

分 类 号:X703[环境科学与工程—环境工程]

 

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