垃圾渗滤液与城市污水同步脱氮影响因素分析  被引量:5

Nitrogen removal in the consolidated treatment of leachate and municipal wastewater

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作  者:石明岩[1] 冯兆继[1] 余建恒 王少林 夏耿东 

机构地区:[1]广州大学土木工程学院,广东广州510006 [2]广州市大坦沙污水处理厂,广东广州510163

出  处:《广州大学学报(自然科学版)》2010年第3期56-59,共4页Journal of Guangzhou University:Natural Science Edition

基  金:广州市科技计划项目(2007J1-Q411)资助

摘  要:采用倒置A2/O工艺同步处理垃圾渗滤液与城市污水脱氮.结果表明:水力停留时间对脱氮影响较为显著,试验条件下水力停留时间至少应维持9 h;好氧池溶解氧浓度增加对总氮去除不利;在60%~100%的范围内提高污泥回流比对有机物和总氮去除有利;混合液回流比对有机物和氨氮的去除基本不产生影响,在100%~200%范围内增加对反硝化有一定促进作用.Nitrogen removal in the consolidated treatment of leachate and municipal wastewater by reversed A2/O process was studied,in the experiment,the results showed that HRT was the key factor for nitrogen removal efficiency.HRT should be long to 9 hours under the test conditions.The dissolved oxygen of the aerobic basin increase is hurt to total nitrogen removal.At the range of 60% to 100%,improving the sludge return ratio could get better organic and denitrification removal treatment effect.At the range of 100% to 200%,improving the mixed-liquor return ratio could get better denitrification removal treatment effect.

关 键 词:倒置A2/O工艺 垃圾渗滤液 城市污水 脱氮 水力停留时间 

分 类 号:X703[环境科学与工程—环境工程]

 

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