A-A^2/O工艺提质改造城市污水厂实践  被引量:4

Practice of Up-to-standard Reconstruction for Sewage Plant by A-A^2/O Process

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作  者:池年平[1,2] 

机构地区:[1]湖南华亿市政工程设计有限公司,湖南长沙410000 [2]同济大学环境科学与工程学院,上海200092

出  处:《佳木斯大学学报(自然科学版)》2011年第3期358-360,364,共4页Journal of Jiamusi University:Natural Science Edition

摘  要:某市D污水处理厂设计时执行《污水综合排放标准》(GB8978-1996)中二级标准,无法达到现行标准《城镇污水处理厂污染物排放标准》(GB 18918-2002)一级B标准对脱氮除磷的要求,且进水具有明显的低C/N特征,为此对污水处理系统进行了改造,新建生物选择池、厌氧池和缺氧池,结合原有的卡罗塞尔氧化沟组成A-A2O工艺,生物选择池可以消除硝化液对厌氧除磷的不利影响,提高后续A2O工艺的脱氮除磷效果,出水水质能稳定达标,该工程可以为老厂脱氮除磷工艺改造提供参考.Second class of the "Integrated Wastewater Discharge Standard"(GB8978-1996) was employed by some projects constructed before 1999.It is unable to meet the current national sanitary standard of first B class of "Municipal Wastewater Treatment Plant discharge standards"(GB 18918-2002) at nitrogen and phosphorus.Water quality parameters of inflow have characteristics of low C/N.Sewage treatment system has been reconstruction for up-to-standard.Bioselection pool,anaerobic tank and Anoxic tank have been construction to combine with Oxidation Ditch to A-A2O Process.Bioselection pool can eliminate the adverse effects of nitrification solution on anaerobic phosphorus and improve the effect of nitrogen and phosphorus removal process for the follow-up A2O.It can provide a reference for the old factory converted into nitrogen and phosphorus removal process.

关 键 词:A-A2/O工艺 低浓度城市污水 提质改造 污水处理厂 

分 类 号:X703.1[环境科学与工程—环境工程]

 

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