汶川百花大桥震害分析与抗震性能研究  被引量:4

Analysis of seismic damage and aseismic behavior of Wenchuan Baihua Bridge

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作  者:雷俊卿[1] 宋力勋[1] 

机构地区:[1]北京交通大学土木建筑工程学院,北京100044

出  处:《北京交通大学学报》2012年第1期1-5,11,共6页JOURNAL OF BEIJING JIAOTONG UNIVERSITY

基  金:国家自然科学基金资助项目(5087820;51178042);高等学校博士学科点专项基金资助项目(20100009110017);交通部西部交通建设科技项目资助(200631822302-07)

摘  要:以遭到严重震害的汶川百花大桥为研究对象,从抗震设计的角度出发,用反应谱法和时程法进行了第一级设防水准(E1)地震作用下的弹性分析,用非线性时程法进行了第二级设防水准(E2)地震作用下的弹塑性分析,并综合分析了该桥的震害原因和抗震性能,为同类桥梁的设计提供参考和借鉴.分析结果表明:双柱式柔性墩的采用导致该桥整体刚度较小;桥墩纵筋和箍筋的配置不足导致了E1地震下的承载力不足,而E2地震下的塑性变形是满足要求的;固定墩处支座设置和系梁布置的不合理导致了固定墩左墩柱受到严重破坏;第五和第六联之间刚度差别较大而牛腿(悬臂支托)的支承长度过小,导致该牛腿处发生了落梁破坏.Wenchuan Baihua Bridge, which was seriously damaged in the earthquake, was chosen as the object of study. Elastic analysis under earthquake action E1 was performed with both response spectrum method and time-history method,and elastoplastie analysis under earthquake action E2 was performed with nonlinear time-history method. In the end, causes of the damage and aseismic behavior of the bridge were summarized in order to provide design references for similar bridges. The studies show that: 1)the use of double-columns flexible piers decreased the integral stiffness; 2)the deficiency of longitudinal bar and stirrup in the piers leads to the low bearing capacity under El, while the plastic deformation under E2 can meet the standard; 3)the unreasonable layout of bearings and tie beams causes the severe damage of the left column of the fixed piers; 4)the small bearing length of the bracket, together with the big stiffness gap between the fifth and sixth continuous beam, lead to the falling down of the superstructure.

关 键 词:百花大桥 震害分析 抗震性能 反应谱分析 时程分析 弹塑性分析 

分 类 号:U442.55[建筑科学—桥梁与隧道工程]

 

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