改良A^2/O分段进水工艺用于污水厂升级改造  被引量:13

Modified Step-feed A^2/O Process for Upgrade and Reconstruction of WWTP

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作  者:朱云鹏[1] 彭永臻[1,2] 王继苗 黄东辉 祝征圣 赵勇 王淑莹[1] 刘旭[1] 

机构地区:[1]北京工业大学环境与能源工程学院,北京100124 [2]哈尔滨工业大学市政环境工程学院,黑龙江哈尔滨150090 [3]青岛开投双元水务有限公司,山东青岛266109 [4]江苏裕隆环保有限公司,江苏无锡214214

出  处:《中国给水排水》2012年第7期22-26,31,共6页China Water & Wastewater

基  金:"十一五"国家科技支撑计划重点项目(2009BAC57B01);国家水体污染控制与治理科技重大专项(2008ZX07317-007-105)

摘  要:采用传统A2/O工艺处理市政污水时出水水质很难达到《城镇污水处理厂污染物排放标准》(GB 18918—2002)的一级A标准。青岛城阳污水处理厂采用改良A2/O分段进水工艺进行升级改造,通过分段进水的形式强化系统对原水中碳源的利用,提高对污染物的去除能力。运行结果表明,经改良后生物池对COD、NH4+-N和TN的去除率分别能够稳定维持在86.25%、95%和66%以上,最终出水平均值分别为38、1.57和13.56 mg/L,满足一级A排放标准;对TP的去除率在81.40%以上,在深度处理时投加少量氯化铁进一步对磷进行去除,出水值也达到了一级A标准。经改良后,生物池出水水质在达到一级A标准的基础上每天可节省电耗约672 kW·h。When the traditional A^2/O process is used to treat municipal wastewater, the effluent quality can hardly meet the first level A criteria specified in Discharge Standard of Pollutants for Municipal Wastewater Treatment Plant (GB 18918 -2002). The modified step-feed A^2/O process was adopted for upgrade and reconstruction of the Qingdao Chengyang WWTP. Adopting step-feeding patterns en- hanced the carbon source use and the removal efficiency of pollutants. The results showed that the remov- al rates of COD, NH4 - N and TN in the biological tank were more than 86.25%, 95% and 66% , re- spectively, and the average effluent concentrations were 38 mg/L, 1.57 mg/L and 13.56 mg/L respectively, meeting the first level A criteria discharge standard. The removal rate of TP was more than 81.40%, and effluent TP concentration satisfied the first level A criteria discharge standard after the addition of iron chloride in the advanced treatment for phosphorus removal. At the same time, the biological tank saved 672 kW · h of power consumption per day.

关 键 词:A2/O工艺 分段进水 升级改造 悬浮填料 一级A标准 节能降耗 

分 类 号:X703[环境科学与工程—环境工程]

 

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