厌氧池-缺氧池-生物滤池处理养猪废水中试研究  被引量:4

STUDY ON PIGGERY WASTEWATER TREATMENT BY SEPTIC TANK-PREDENITRIFICATION ANAEROBIC TANK-AEROBIC BIOLOGICAL FILTER IN A PILOT SCALE

在线阅读下载全文

作  者:徐振龙[1,2] 陈繁荣[1] 

机构地区:[1]中国科学院广州地球化学研究所,广东广州510640 [2]中国科学院大学,北京100049

出  处:《水处理技术》2014年第12期100-103,114,共5页Technology of Water Treatment

基  金:中国科学院知识创新工程重要方向性项目(KZCX2-YW-JC105)

摘  要:针对养猪场水冲粪工艺悬浮物含量高、水量不稳定的特性,采用二级沉淀的前处理工艺,选择厌氧池-缺氧池-好氧生物滤池作为主体单元,通过好氧出水回流方式强化系统的脱氮性能。根据实验数据分析比较不同进水负荷、回流比条件下污染物的去除情况,并且对不同实验参数的能耗进行了量化。启动后,COD与NH4+-N容积负荷分别可达12 kg/(m3·d)与0.64 kg/(m3·d)。在300%回流体积比的运行条件下,系统整体效能最高,COD、NH4+-N、TN去除率分别为97.6%、82.8%、85.0%,能耗为0.95 k Wh/m3。Based on the characteristics of high suspended solid,flux in piggery wastewater flow,two connected settling tank and a series of anaerobic tankpredenitrification tank-aerobic biological filter were selected as the pretreatment process and main part in this experiment,respectively. This configuration and aerobic output refluxing were expected to strengthen its denitrification efficiency. Pollutant removal efficiency were compared with each other according to the data under different hydraulic loading and reflux ratio,and a quantitative analysis of power consumption was carried out at the same time. After the start-up,COD and ammonia volumetric loading reached as much as 12.0 kg/(m^3·d),0.64 kg/(m^3·d). When the reflux volume ratio was 300%,entire efficiency reached its peak,and power consumption was 0.95 kWh/m^3. Removal efficiency of COD,NH4^+-N,TN was 97.6%,82.8%,85.0%,respectively.

关 键 词:生物滤池 养猪废水 回流比 脱氮 

分 类 号:X713[环境科学与工程—环境工程]

 

参考文献:

正在载入数据...

 

二级参考文献:

正在载入数据...

 

耦合文献:

正在载入数据...

 

引证文献:

正在载入数据...

 

二级引证文献:

正在载入数据...

 

同被引文献:

正在载入数据...

 

相关期刊文献:

正在载入数据...

相关的主题
相关的作者对象
相关的机构对象