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作 者:吴明[1] 王军[1] 李应江[1] 龙胜平[1] 尹丰[1] 鲍磊[1]
机构地区:[1]马鞍山钢铁股份有限公司第一钢轧总厂,安徽马鞍山243000
出 处:《炼钢》2015年第1期17-21,共5页Steelmaking
摘 要:为了达到低磷钢对成品磷质量分数小于0.010%的要求,根据温度、炉渣碱度、渣中w(FeO)以及搅拌等对钢液脱磷的影响,马鞍山钢铁股份有限公司120t转炉应用烟气分析动态控制炼钢技术,采用留渣双渣操作法,制定合理的装入、造渣、供氧制度,优化脱磷参数,通过500多炉次实践对比分析,确定合适的倒炉温度为1540~1580℃,w(C)=0.10%~0.25%,终渣碱度3.0~3.5,w(FeO)=15%~23%,及适合的搅拌强度以达到脱磷率95.2%良好效果,实现了转炉出钢磷质量分数小于0.007%,以及终点碳温双命中96.4%的目标。In order to make the requirement of phosphorus mass fraction less than 0. 010 % for low phosphorous steel, and according to the effect of temperature, slag basicity, w (FeO) of slag and mixing parameters on dephosphorization, the offgas analysis dynamic control steelmaking model was applied on 120 t BOF of Maanshan Iron Steel Company Limited. "Slag-Remaining + Double-Slag" technology, suitable loading system, slagging system and oxygen supply system, optimizing dephosphorization parameter were used in steelmaking. Through the analysis and comparison of 500 experiments, dephosphorization rate 95.2 % can be achieved by taking measures such as the temperature and the carbon mass fraction of the first turning down 1 540 - 1 580 %C and 0. 10 % - 0. 25 %, final slag basicity 3.0 - 3.5, w(FeO) = 15 % - 23 %, and suitable stirring intensity. And the phosphorus mass fraction of converter tapping is less than 0. 070 % and the hit rates of carbon contdnt and temperature both meet the requirement of 96.4 %.
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