油田提高注汽锅炉蒸汽出口干度技术研究  被引量:2

Study on the Technology to Improve the Boiler Outlet Steam Dryness

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作  者:潘立生 张海莹[2] 

机构地区:[1]新疆油田公司工程技术公司,新疆克拉玛依834000 [2]胜利油田石油化工总厂,山东东营257600

出  处:《当代化工》2015年第1期165-167,共3页Contemporary Chemical Industry

摘  要:新疆油田超稠油开发和普通稠油后期开采需要更高的蒸汽干度,而常规锅炉蒸汽出口干度只有80%,已不能满足现阶段注蒸汽开采工艺要求。为此,提出了汽水分离、过热、掺混方法进提高蒸汽干度,并使其伴有15℃过热度,达到了蒸汽驱稠油热采条件,现场应用表明该方法在节能、环保和能效上效果显著。Ultra heavy oil development and ordinary heavy oil late-stage development require higher steam dryness in Xinjiang oilfield. Conventional boiler steam outlet dryness is only 80%, which cannot meet the requirements of the present stage steam injection process. So steam-water separation and overheating and blending method has been used to improve the steam dryness. The treated steam accompanied by 15 ℃ superheat can meet the requirements of the heavy oil thermal recovery. Field application shows that the method is energy conservation and environmental protection, and its energy efficiency is significant.

关 键 词:稠油开发 蒸汽干度 蒸汽开发 汽水分离 

分 类 号:TE357[石油与天然气工程—油气田开发工程]

 

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