生物质电厂SCR脱硝催化剂失效及再生研究  被引量:7

Deactivation mechanism and regeneration of SCR denitration catalyst served in biomass power plant

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作  者:何发泉 王宝冬 马少丹 马子然 马静 刘子林 林德海 孙琦 徐文强 HE Fa-quan WANG Bao-dong MA Shao-dan MA Zi-ran MA Jing LIU Zi-lin LIN De-hai SUN Qi XU Wen-qiang(National Institute of Clean-and-Low-Carbon Energy, Beijing 102209, China)

机构地区:[1]北京低碳清洁能源研究所,北京102209

出  处:《现代化工》2017年第8期72-76,共5页Modern Chemical Industry

基  金:国家"863"计划项目(2012AA06A115);神华集团重大项目(ST30015SH07)

摘  要:对某生物质电厂蜂窝SCR脱硝催化剂失效原因和再生工艺进行了研究。结果表明,该催化剂失活的主要原因是由于催化剂堵孔率超过了50%,灰分造成催化剂实际反应面积大大减少;灰分中含有的碱金属及碱土金属破坏了催化剂表面酸性位,降低了催化剂活性而使催化剂中毒。根据催化剂失活机理,对其再生工艺进行了探索,中试实验结果表明:在一定的条件下,通过吹灰、清洗、酸洗、活性补充和煅烧,可将催化剂活性恢复到工业使用要求。An in-depth study on the deactivated mechanism and regeneration method of SCR de-NOxhoneycomb catalyst for a biomass power plant is carried on.Results show that the deactivation is mainly caused by two reasons as the following:( 1) Catalyst blockage.Blinding rate of the deactivated catalysts exceeds 50%.Fly ash causes the actual reaction area of catalyst to reduce greatly.( 2) Alkalosis.Blinding ash containing alkali metal and alkaline earth metal damages the surface acid sites of catalyst,reducing the activity of catalyst and making it poisoned. According to the mechanism of catalyst deactivation,the regeneration process is hence developed. And the pilot shows that through soot-blowing,cleaning,pickling,activity supplementing and burning under certain conditions,the activity of catalyst can recover and meet the industrial service requirements.

关 键 词:脱硝催化剂 生物质电厂 失活 再生 

分 类 号:TQ426[化学工程]

 

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