采用给水加热实现660MW超临界机组宽负荷脱硝的理论研究  被引量:19

Theoretical Study on Wide Load Denitration of a 660MW Supercritical Unit by Retrofitting the Feedwater Heating System

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作  者:张国柱 李冰心 李亚维 李飞 李本锋 刘继平[2] 

机构地区:[1]大唐(北京)能源管理有限公司,北京100097 [2]西安交通大学能源与动力工程学院,西安710049

出  处:《动力工程学报》2018年第1期50-54,共5页Journal of Chinese Society of Power Engineering

基  金:国家重点基础研究发展计划资助项目(2015CB251504);国家自然科学基金资助项目(51436006;51476128)

摘  要:为了解决燃煤机组低负荷运行时脱硝效率低、热经济性差的问题,以某660MW超临界机组为例,对采用蒸汽喷射器的低负荷给水加热系统进行改进,添加了喷射器旁路和高低压蒸汽入口调节阀,以实现宽负荷脱硝.计算得到No.0高压加热器的温升范围,以及高负荷时喷射器的运行优化方法.结果表明:在满足脱硝及省煤器稳定运行的条件下,当机组负荷高于30%负荷时,No.0高压加热器可选温升范围较大,可根据脱硝要求选择合适的给水温升;当机组高负荷运行时,可降低喷射器入口高压蒸汽压力,提高机组热经济性.To improve the denitration efficiency and thermodynamic performance of a 660 MW supercritical unit operating at low load, a bypass line and high/low-pressure steam regulating valves were added to its original low-load feedwater heating system including a steam ejector, so as to achieve wide load denitration of the unit. The temperature rise of No. 0 high pressure heater was calculated, while the operation mode of the steam ejector operating at high load was optimized. Results show that for the unit load greater than 30%, the No. 0 high pressure heater has a large range of temperature rise to satisfy the denitration require ment. When the unit operates at high load, the thermal efficiency of the unit could be improved by reduc ing the pressure of high-pressure steam at inlet of the steam ejector.

关 键 词:给水加热 蒸汽喷射器 宽负荷脱硝 热经济性 

分 类 号:TM621[电气工程—电力系统及自动化]

 

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