深床过滤应用于垂直流人工湿地净化效果与堵塞研究  

Study on the Purification and Clogging Performance of Deep-bed Filtration Applied in Vertical Flow Constructed Wetland

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作  者:王媚[1,2] 徐栋 王晓莹[1,2] 陈迪松 武俊梅 张义[1] 周巧红[1] 肖恩荣[1] 张婷[1,3] 吴振斌[1] WANG Mei;XU Dong;WANG Xiaoying;CHEN Disong;WU Junmei;ZHANG Yi;ZHOU Qiaohong;XIAO Enrong;ZHANG Ting;WU Zhenbin(State Key Laboratory of Freshwater Ecology and Biotechnology,Institute of Hydrobiology,Chinese Academy of Sciences Wuhan 430072)

机构地区:[1]中国科学院水生生物研究所淡水生态与生物技术国家重点实验室,武汉430072 [2]武汉地产开发投资集团有限公司,武汉430022 [3]中国科学院大学,北京100049

出  处:《工业安全与环保》2018年第8期81-84,共4页Industrial Safety and Environmental Protection

基  金:湖北省自然科学基金青年科学基金(2014CFB282);湖北省环保厅科研专项(2015HB14);湖北省技术创新专项软科学研究类项目(2016ADC101)

摘  要:在序批式工况下,研究了深床过滤型垂直流人工湿地(深度1.5 m,C系统)相对常规0.5 m(A系统)和1.0 m床深(B系统)湿地对进水中主要污染物的净化效果和堵塞过程。结果表明,C系统污染物整体去除效果最优。A,B,C系统分别在运行约140,155,175天后严重堵塞,各系统总处理水量A B C=1.0 2.1 3.2,深床过滤垂直流人工湿地能一定程度延缓湿地堵塞,增加水处理量,水力负荷一定时,可有效减少湿地建设面积。The purification efficiency of main pollutants and clogging process of deep - bed filtration ( 1.5 m, system C) vertical flow constructed wetland (VFCW) compared with conventional 0.5 m ( system A) and 1.0 m deep bed ( system B) VFCWs under continuous batch condition has been investigated. The results show that the overall removal efficiency of pollutants of system C is better than that of system A and B. Systems A, B and C are se- riously clogged after operated for about 140, 155, 175 days respectively, and the ratio of total wastewater treated for the systems is : A : B : C = 1.0 : 2.1 : 3.2. Thus, the deep - bed filtration VFCW can delay the clogging process to certain extent and increase the amount of wastewater treated, and under set hydraulic load, it can effectively reduce the wetland construction area.

关 键 词:人工湿地 深床过滤 净化 堵塞 建设面积 

分 类 号:X703[环境科学与工程—环境工程]

 

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