产水气井高效廉价排水采气技术的研究与应用  被引量:8

Research and application of efficient and economic draining and gas-recovery technique for water-producing natural gas well

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作  者:郭东红[1,2] 杨晓鹏[1,2] 孙建峰[1,2] 崔晓东[1,2] 侯庆锋 GUO Dong-hong;YANG Xiao-peng;SUN Jian-feng;CUI Xiao-dong;HOU Qing-feng(Oilfield Chemistry Department,Research Institute of Petroleum Exploration & Development of PetroChina,Beijing 100083,China;CNPC Key Laboratory of Oilfield Chemistry,Beijing 100083,China)

机构地区:[1]中国石油勘探开发研究院油田化学研究所,北京100083 [2]中国石油天然气集团公司油田化学重点实验室,北京100083

出  处:《现代化工》2018年第10期137-139,共3页Modern Chemical Industry

基  金:中国石油勘探与生产分公司资助项目"排水采气化学剂的研究与应用"(2012kt302)

摘  要:为解决苏里格气田不断出现的井筒积液难题,根据其气藏特点,研制出一种新的高效廉价泡排剂配方体系KPJ-15。测试结果表明,在煤油质量分数为0~15%、矿化度为30 000 mg/L的条件下,KPJ-15体系的起始发泡量、析液半衰期以及携液量均高于现场用泡排剂。泡排现场试验结果表明,KPJ-15泡排剂体系具有较好的排液和增产效果。In order to solve the problem of wellbore liquid accumulation in Sulige gas field,a new,efficient and cheap foam draining agent KPJ-15 is prepared according to the characteristics of gas reservoir.The test results reveal that initial foaming volume,half-life of drainage and liquid-carrying amount of KPJ-15 are far higher than those of present foam draining agents under conditions that the concentration of kerosene is in the range of 0%-15% and the salinity is 30 000 mg·L^-1.Preliminary spot tests verify that foam draining agent KPJ-15 achieves good results of drainage effect and can increase gas production.

关 键 词:气井积液 泡沫排水剂 发泡性能 析液半衰期 现场应用 

分 类 号:TE377[石油与天然气工程—油气田开发工程]

 

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