Experimental study on film cooling performance of imperfect holes  被引量:11

Experimental study on film cooling performance of imperfect holes

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作  者:Ke'nan HUANG Jingzhou ZHANG Xiaoming TAN Yong SHAN 

机构地区:[1]College of Energy and Power Engineering, Jiangsu Province Key Laboratory of Aerospace Power System, Nanjing University of Aeronautics and Astronautics, Nanjing 210016, China [2]Collaborative Innovation Center for Advanced Aero-Engine, Beijing 100083, China

出  处:《Chinese Journal of Aeronautics》2018年第6期1215-1221,共7页中国航空学报(英文版)

基  金:the financial support for this project from the National Natural Science Foundation of China (Nos.51276090 and U1508212)

摘  要:An experimental study is made to investigate the film cooling performance of imperfect holes due to in-hole blockage over a flat plate. A specifically pyramid-shaped element is used to simulate the in-hole blockage. Six in-hole blockage orientations(such as leading-inlet, leading-middle,leading-exit, trailing-inlet, trailing-middle and trailing-exit) and four blocking ratios(ranging from 0.1 to 0.4) are taken into considerations. Based on the experimental results, the influences of in-hole blockage on the film cooling effectiveness and discharge coefficient under typical blowing ratios are analyzed. It is confirmed that the in-hole blockage results in a reduction of discharge coefficient related to the perfect film cooling holes, especially for the leading-exit and trailing-inlet orientations with a big blocking ratio. However, in the view of film cooling effectiveness, the in-hole blockage shows complicated affecting roles. In general, except for the leading-exit orientation, the in-hole blockages produce detrimental influence on the film cooling effectiveness.An experimental study is made to investigate the film cooling performance of imperfect holes due to in-hole blockage over a flat plate. A specifically pyramid-shaped element is used to simulate the in-hole blockage. Six in-hole blockage orientations(such as leading-inlet, leading-middle,leading-exit, trailing-inlet, trailing-middle and trailing-exit) and four blocking ratios(ranging from 0.1 to 0.4) are taken into considerations. Based on the experimental results, the influences of in-hole blockage on the film cooling effectiveness and discharge coefficient under typical blowing ratios are analyzed. It is confirmed that the in-hole blockage results in a reduction of discharge coefficient related to the perfect film cooling holes, especially for the leading-exit and trailing-inlet orientations with a big blocking ratio. However, in the view of film cooling effectiveness, the in-hole blockage shows complicated affecting roles. In general, except for the leading-exit orientation, the in-hole blockages produce detrimental influence on the film cooling effectiveness.

关 键 词:Discharge coefficient Experimental test Film cooling effectiveness Heat transfer In-hole blockage 

分 类 号:TK124[动力工程及工程热物理—工程热物理]

 

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