新型高含油污泥携带量的KG-1调剖堵剂制备与性能评价  

Preparation and performance evaluation of profile modificator based on oily sludge

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作  者:易永根[1] 申坤[1] 候军刚 罗庆梅[1] 师现云 赖小娟[2] YI Yong-gen;SHEN Kun;HOU Jun-gang;LUO Qing-mei;SHI Xian-yun;LAI Xiao-juan(Oil Production Plant 1 of PetroChina Changqing Oilfield Company,Yan’an 716000,China;Shaanxi Key Laboratory of Chemical Additives for Industry,Shaanxi University of Science and Technology,Xi’an 710021,China)

机构地区:[1]长庆油田分公司第一采油厂,陕西延安716000 [2]陕西科技大学陕西省轻化工助剂重点实验室,陕西西安710021

出  处:《应用化工》2019年第3期529-532,共4页Applied Chemical Industry

基  金:国家自然科学基金(51103081);陕西省教育厅重点实验室项目(17JS012);陕西省工业科技攻关项目(2016GY-193)

摘  要:为了更加妥善地处理石油开采过程中产生的含油污泥,选择一种新型疏水缔合聚丙烯酰胺HAPE作为稠化剂,制备了一种含油污泥携带量达到40%的调剖堵剂,并对其进行性能评价和人造岩心封堵模拟实验。结果表明,在长期保温和剪切条件下,该堵剂的表观粘度变化不大,耐温耐剪切性能良好,在储层温度60℃下持续老化3个月,体系未出现脱水现象,表现出较好的长期热稳定性能;在完成封堵后,人造岩心渗透率迅速下降,封堵率达94%以上,经过50 PV的地层水的连续注入后,堵剂的岩心封堵率仍然大于93%,耐冲刷性能良好。In order to improve the handling capacity of oily sludge produced during petroleum exploitation,a high-performance profile modificator with 40% oily sludge was prepared by using hydrophobic association polyacrylamide HAPE as thickener.Performance evaluation of the profile modificator and plugging test for artificial cores were performed.The results showed that the profile modificator has good temperature-tolerate and shear-tolerate properties.After retrogradation tested for three months under reservoir temperature at 60 ℃,the phenomenon of dehydration did not appear and the system exhibited good thermal stability.The permeability of artificial cores decreased after plugging and the plugging rate was over 94%.The plugging rate was over 93% after displaced with 50 PV brine,indicating the profile modificator has good erosion resistance properties.

关 键 词:含油污泥 堵剂 性能研究 封堵率 

分 类 号:TQ317[化学工程—高聚物工业] TE357[石油与天然气工程—油气田开发工程]

 

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