检索规则说明:AND代表“并且”;OR代表“或者”;NOT代表“不包含”;(注意必须大写,运算符两边需空一格)
检 索 范 例 :范例一: (K=图书馆学 OR K=情报学) AND A=范并思 范例二:J=计算机应用与软件 AND (U=C++ OR U=Basic) NOT M=Visual
作 者:刘永红[1] 党康 王宁[1] 李耀中 李妙婕 王毅博[1] 张豪 蔡经栋 LIU Yonghong;DANG Kang;WANG Ning;LI Yaozhong;LI Miaojie;WANG Yibo;ZHANG Hao;CAI Jingdong(College of Environmental and Chemical Engineering,Xi′an Polytechnic University,Xi′an 710048;Shaanxi Luhuan Environmental Engineering Co.Ltd.,Xi′an 710002;Shishi Lanlingdun Printing and Dyeing Co.Ltd.,Quanzhou 362700)
机构地区:[1]西安工程大学环境与化学工程学院,西安710048 [2]陕西陆环环保工程有限公司,西安710002 [3]石狮市蓝灵顿印染有限公司,泉州362700
出 处:《环境科学学报》2019年第10期3350-3355,共6页Acta Scientiae Circumstantiae
基 金:国家自然科学基金(No.21176197);陕西省科技统筹创新工程计划项目(No.2011KTZB03-03-01);陕西省科技厅工业攻关项目(No.2008k07-14);陕西省教育厅专项科学研究计划项目(No.19JK0370);石狮市科技公共服务平台产学研项目(No.003)
摘 要:针对泉州某印染厂实际废水(COD 800~1800 mg·L^-1,NH+4^-N 20~50 mg·L^-1,pH=8~14),以两种新型载体分别作为厌氧与好氧单元中微生物固定化载体,考察了中试规模上流式厌氧污泥床反应器(UASB)与柔性悬浮载体移动床生物膜反应器(SCMBBR)组合工艺对该废水的处理效果.4个月的连续试验结果表明:①经过30 d前期调试运行该工艺系统成功启动,处理量为1.5~2.2 m^3·d^-1时,AMC/UASB和SCMBBR反应器对COD的去除率分别达到22%和50%,AMC/UASB反应器出现明显的产气现象,SCMBBR中载体挂膜状况良好;②启动完成后经过90 d的连续运行,当AMC/UASB和SCMBBR反应器水力停留时间分别为10.7 h和8.8 h,废水处理量为5 m^3·d^-1时,稳定运行阶段整个工艺废水COD去除率达到78%,出水氨氮平均浓度为3.4 mg·L^-1;此外,整体工艺色度去除率达到65%,其中,厌氧段色度去除率达到50%左右;③通过分析计算,整个系统污泥减量达到67.7%~76.6%,该生物组合工艺具有明显的污泥减量效果.Two kinds of novel carriers were used as microbial immobilization media in a combined up-flow anaerobic sludge bed(UASB) and aerobic moving bed biofilm reactor(SCMBBR) pilot-scale process to treat wastewater(COD 800~1800 mg·L^-1, NH+4^-N 20~50 mg·L^-1, pH=8~14) from a printing and dyeing plant in Quanzhou. After nearly 4 months of continuous operation, it is found that:①The process system was successfully started up after 30 days. When the loading was 1.5~2.2 m^3·d^-1, the removal rates of COD in AMC/UASB and SCMBBR reactors were 22% and 50%, respectively. The gas production in AMC/UASB reactor was obvious, and the biofilm on carriers in the SCMBBR reactor were well developed. ②After 90 days of operation, when the hydraulic retention time of AMC/UASB and SCMBBR were 10.7 h and 8.8 h respectively, with the VLR at 5 m^3·d^-1, the removal rate of COD achieved 78%, and the average concentration of ammonia nitrogen in the effluent was around 3.4 mg·L^-1. In addition, the removal rate of chroma by the combined process was 65%, while the anaerobic color removal rate was about 50%. ③According to the analysis, the residual sludge reduction rate of the combined process reached 67.6%~76.6%, indicating the composite process had a good performance on sludge reduction.
关 键 词:AMC载体 PGB载体 SCMBBR 色度 污泥减量 印染废水
分 类 号:X703.1[环境科学与工程—环境工程]
正在载入数据...
正在载入数据...
正在载入数据...
正在载入数据...
正在载入数据...
正在载入数据...
正在载入数据...
正在链接到云南高校图书馆文献保障联盟下载...
云南高校图书馆联盟文献共享服务平台 版权所有©
您的IP:216.73.216.249