潮州某污水厂A/O氧化沟工艺不停产提标扩容改造  被引量:9

Upgrading and Expansion without Shutdown of a WWTP in Chaozhou with A/O Oxidation Ditch Process

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作  者:杨登 袁敏忠 钟毓 苏文越 YANG Deng;YUAN Min-zhong;ZHONG Yu;SU Wen-yue(GDEP Engineering Research&Design Institute Co.Ltd.,Guangzhou 510000,China)

机构地区:[1]广东省环境保护工程研究设计院有限公司,广东广州510000

出  处:《中国给水排水》2020年第20期119-123,共5页China Water & Wastewater

摘  要:潮州某污水处理厂原规模为10×10^4m^3/d,采用A/O机械曝气氧化沟工艺,出水标准为《城镇污水处理厂污染物排放标准》(GB 18918-2002)一级B标准。提标扩容工程在不新增用地及不停产的条件下,将出水标准提升至一级A标准和广东省地方标准《水污染物排放限值》(DB 44/26-2001)第二时段一级排放标准中较严值,并将规模扩建至15×10^4m^3/d。提标改造工程在原A/O机械曝气氧化沟基础上新增曝气生物滤池+反硝化深床滤池的深度处理工艺,扩容工程采用A/A/O-MBR+紫外消毒处理工艺。实际运行结果表明,提标扩容工程运行良好,出水水质稳定达标。The original treatment capacity of a WWTP in Chaozhou is 10×10^4 m^3/d,adopting A/O mechanical aeration oxidation ditch process,and the effluent standard is the first level B standard in the Discharge Standard of Pollutants for Municipal Wastewater Treatment Plant(GB 18918-2002).Under the condition of no new land usage and no production stopping,the standard of effluent should be raised to the stricter value between the first level A standard(GB 18918-2002)and the first level discharge standard in the second period of the local standard of Guangdong Province Discharge Limits of Water Pollutants(DB 44/26-2001),and the scale should be expanded to 15×10^4 m^3/d.The advanced treatment process of biological aerated filter+denitrification deep bed filter was added on the basis of the original A/O mechanical aeration oxidation ditch in the upgrading project,and the A/A/O-MBR+UV disinfection process was adopted in the expansion project.The actual operation results showed that the operation of the project was good and the effluent quality was stable.

关 键 词:不停产改造 曝气生物滤池 反硝化深床滤池 A/A/O-MBR 

分 类 号:TU992.3[建筑科学—市政工程]

 

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