改良曝气生物滤池工艺应急处理雨水调蓄池污水  被引量:1

Emergency treatment of rainwater storage tank wastewater by modified biological aerated filter process

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作  者:胡天媛[1] 孟令鑫[1] 侯红勋[1] 李涛[1] 张静[1] HU Tian-yuan;MENG Ling-xin;HOU Hong-xun;LI Tao;ZHANG Jing(Anhui Guozhen Environmental Protection Technology Joint Stock Co.,Ltd.,Hefei 230088,China)

机构地区:[1]安徽国祯环保节能科技股份有限公司,合肥230088

出  处:《工业用水与废水》2020年第6期25-28,共4页Industrial Water & Wastewater

基  金:国家水体污染控制与治理科技重大专项(2015ZX07218001)。

摘  要:针对雨水调蓄池进水水量波动大、氨氮浓度偏高、COD浓度偏低的特点,采用改良曝气生物滤池工艺进行处理。试验结果表明:进水COD质量浓度从84 mg/L以内下降到44 mg/L以下,氨氮质量浓度从5.3-24.4 mg/L下降至0.09-1.20 mg/L,TP质量浓度从0.08-1.36 mg/L下降到0.04-0.40 mg/L,改良曝气生物滤池工艺对COD、氨氮、TP等去除率分别约为33.5%、96%、55%,出水水质达到GB 3838—2002《地表水环境质量标准》Ⅴ类标准。According to the characteristics of rainwater storage tank such as:large fluctuation of water quantity,high concentration of ammonia nitrogen,low concentration of COD and so on,an improved biological aerated filter process was adopted for its treatment.The experimental results showed that;the mass concentration of COD in influent water decreased from not above 84 mg/L to below 44 mg/L,the mass concentration of ammonia nitrogen decreased from 5.3-24.4 mg/L to 0.09-1.20 mg/L,the mass concentration of TP decreased from 0.08-1.36 mg/L to 0.04-0.40 mg/L.The removal rates of COD,ammonia nitrogen and TP by the said modified biological aerated filter process were 33.5%,96%and 55%respectively,the effluent water quality met the requirement of class V of GB 3838—2002 Surface water environmental quality standard.

关 键 词:预处理 改良 曝气生物滤池 应急处理 雨水 调蓄池 

分 类 号:X703.1[环境科学与工程—环境工程]

 

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