渝东南地区页岩气井废水来源分析及处理措施  

Sources Analysis and Treatment Measures of Shale Gas Well Wastewater in Southeast Chongqing Area

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作  者:靳雅夕 包凯[2] 彭柳 孙婧榕 陈建文 范小俊 徐辉 JIN Ya-xi;BAO Kai;PENG Liu;SUN Jing-rong;CHEN Jian-wen;FAN Xiao-jun;XU Hui(SINOPEC East China Oil&Gas Company Experimental Research Center,Jiangsu Yangzhou 225007;SINOPEC East China Oil&Gas Company Chongqing Shale Gas Co.,Ltd.,Chongqing 408400,China)

机构地区:[1]中国石油化工股份有限公司华东油气分公司实验研究中心,江苏扬州225007 [2]中国石化华东油气分公司重庆页岩气有限公司,重庆408400

出  处:《广州化工》2021年第1期79-82,共4页GuangZhou Chemical Industry

摘  要:本文根据重庆渝东南工区A钻井平台的实际情况,分析了其污水的来源及特征,研究了其废水处理的两种方式:处理后回用或处理后外排,其中着重介绍了MBR工艺在外排水处理中的运用。通过对回用水出水水质监测得到:pH为6.8~7.6,悬浮物为38~47 mg/L,氯离子为685~13900 mg/L,满足回用要求。通过对外排水出水水质监测得到:pH为6.6~7.3,COD为44~88 mg/L,氨氮为0.17~1.78 mg/L,达到国家《污水综合排放标准》的一级排放标准,处理方案在类似油田中具有推广价值。Based on the actual situation of a drilling platform in the southeast working area of Chongqing,the source and characteristics of its sewage were analyzed,and two ways of wastewater treatment were studied:reuse after treatment or efflux after treatment.The application of MBR process in external drainage treatment was emphatically introduced.By analyzing the reclaimed water,the results showed that the pH value was 6.8~7.6,the suspended solid was 38~47 mg/L,and the chloride ion was 685~13900 mg/L,which met the recycling requirements.According to the water quality analysis of the external drainage,the pH was 6.6~7.3,COD was 44~88 mg/L,and ammonia nitrogen was 0.17~1.78 mg/L,which reached the first level of the national sewage comprehensive discharge standard.The treatment scheme has the value of promotion in similar oil fields.

关 键 词:页岩气 废水 回用水 MBR工艺 外排水 

分 类 号:X52[环境科学与工程—环境工程]

 

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