油水井封堵剂(粉体暂堵剂)压井液在涩北气田的应用  被引量:1

APPLICATION OF OIL-WATER WELL PLUGGING AGENT(POWDER TEMPORARY PLUGGING AGENT)AND WELL CONTROL FLUID IN SEBEI GAS FIELD

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作  者:章志轩 冶克杰 李子建 欧宝明 何正林 任世霞 Zhang Zhixuan;Ye Kejie;Li Zijian;Ou Baoming;He Zhenglin;Ren Shixa(Drilling and Production Technology Research Institute of Petro China Qinghai Oilfield Company,Dunhuang 736200,Gansu,China;Downhole Operation Company of Petro China Qinghai Oilfield Company,Mangya 816400,Qinghai,China)

机构地区:[1]中国石油青海油田分公司钻采工艺研究院,甘肃敦煌736200 [2]中国石油青海油田分公司井下作业公司,青海茫崖816400

出  处:《精细石油化工》2022年第5期20-22,共3页Speciality Petrochemicals

基  金:青海油田公司科技项目(2021T12)。

摘  要:针对涩北气田储层特性,对YH-01压井液暂堵剂压井液进行了室内评价和现场应用。结果表明:该压井液暂堵成功率高、复产率高、费用低及现场配液方便,现场累计试验52井次,井平均压力系数0.66,试验后井均漏速降低90%以上,气井复产率可达85%。According to the reservoir characteristics of Sebei gas field,YH-01 kill fluid(temporary plugging agent kill fluid)was evaluated in laboratory and applied in field.The results show that the well killing fluid has high success rate of plugging,high recovery rate,low cost and convenient on-site liquid preparation.The field test has been conducted for 52 wells,and the average pressure coefficient of the well is 0.66.After the test,the average leakage rate of the well is reduced by more than 90%,and the recovery rate of the gas well can reach 85%.

关 键 词:涩北气田 低压气井 油水井封堵剂 暂堵压井液 现场试验 

分 类 号:TE358[石油与天然气工程—油气田开发工程]

 

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