基于电机悬置优化技术的轻型火箭炮发射底盘减隔振技术研究  

Research on the Vibration Reduction and Isolation Technology of Light Rocket Launcher Chassis Based on Motor Mount Optimization

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作  者:刘彦臣[1,2] 黄雪涛[3] LIU Yanchen;HUANG Xuetao(School of Mechanical and Electrical Engineering,North University of China,Taiyuan 030051,Shanxi,China;Institute of Military-civilian Integration and Innovation,North University of China,Taiyuan 030051,Shanxi,China;Department of Automotive Engineering,Shandong Jiaotong University,Jinan 250357,Shandong,China)

机构地区:[1]中北大学机电工程学院,山西太原030051 [2]中北大学军民融合协同创新研究院,山西太原030051 [3]山东交通学院汽车工程学院,山东济南250357

出  处:《火炮发射与控制学报》2023年第2期14-19,共6页Journal of Gun Launch & Control

基  金:创新特区项目(20-163-00-TS-006-006-05)。

摘  要:针对某轻型火箭炮发射底盘的低频异常振动问题,采用理论推导、仿真分析和试验验证相结合的方法,进行了轻型火箭炮发射底盘异常振动测试,构建了包括电机悬置参数在内的火箭炮发射底盘振动理论模型和有限元仿真模型,分析了火箭炮发射底盘电机悬置的隔振效果,结合试验结果和理论计算结果,完成了电机悬置的优化设计,并通过电机悬置优化前后的轻型火箭炮发射底盘在炮弹装载过程中的振动试验对比,验证了电机悬置优化的减振效果。试验结果表明:采用电机悬置优化方案后,载运装置的振动情况得到明显改善,装载导轨处的振动功率谱密度峰值由原来的0.67 m/s^(2)下降到0.33 m/s^(2),比优化前降低了50.7%,有效地改善了轻型火箭炮发射底盘的低频异常振动现象。In order to solve the problem of abnormal low frequency vibration of light rocket launcher chassis,this paper combines theoretical derivation,simulated analysis and experimental verification to measure the abnormal vibration of light rocket launchers.A vibration theoretical model and finite element simulation model of rocket launcher chassis including motor mounting parameters is established.And the vibration isolation effect of the rocket launcher chassis motor mount is analyzed.Based on experimental and theoretical calculation results,the design of the motor suspension is optimized.Through the comparison of vibration sustained by the rocket launcher chassis during loading before and after the mounting optimization,the vibration reduction effect of the motor mount optimization is verified.The experiment result shows that after using the optimal design of the motor suspension,vibration sustained by the chassis has obviously improved with the peak value of vibration power spectral density of the loading guide rails reduced from 0.67 m/s^(2)to 0.33 m/s^(2),50.7%lower than before the optimization,which effectively improves the abnormal low frequency vibration phenomenon of light rocket launcher chassis.

关 键 词:电机悬置 优化技术 减振技术 有限元仿真 

分 类 号:TJ012[兵器科学与技术—兵器发射理论与技术]

 

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