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作 者:徐文娟 解传昕 杨洪涛 张浩 徐玉霞 张洁 Xu Wenjuan;Xie Chuanxin;Yang Hongtao;Zhang Hao;Xu Yuxia;Zhang Jie(Tianjin Branch CNOOC(China)Co.,LTD.,Tianjin 300450,China)
机构地区:[1]中海石油(中国)有限公司天津分公司,天津300450
出 处:《精细石油化工》2024年第5期6-10,共5页Speciality Petrochemicals
基 金:中海石油(中国)有限公司重大项目基金(KJZH-2024-2204)。
摘 要:针对水平注水井调剖过程中注入压力高,措施效果差的问题,以渤海X油田为目标,建立了低相对分子质量、低初黏的双低乳液丙烯酰胺冻胶调剖体系.室内性能评价实验表明:物模试验注入压力仅为常规冻胶调剖体系的5833%,调剖后,当水平段的趾部是高渗时,高渗岩心管分流量由调剖前的925%下降至583%,调剖效果较好.当水平段跟部为高渗时,高渗岩心管分流量由调剖前的912%下降至439%,高、低渗透管的分流量出现反转;调剖效果进一步好转.该体系在渤海X油田E井组进行了现场应用,措施后含水率最高下降52%,累计增油13786m^(3).Aiming at the problems of high injection pressure and poor effect of measures in profile control of horizontal water injection wells,a profile control system of double-low emulsion polyacrylamide gel with low molecular weight and low initial viscosity was developed for Bohai X oilfield.Laboratory performance evaluation experiments showed that the injection pressure of the physical model test was only 58.33% of that of the conventional gel profile control system.After profile control,when the toe of the horizontal section was high permeability,the flow ratio of the hyperosmotic core tube decreased from 92.5% before profile control to 58.3%,and the profile control effect was good.When the heel of the horizontal section was high permeability,the flow ratio of the high permeability core tube decreased from 91.2% before profile control to 43.9%,and the flow ratio of the high and low permeability tubes reversed.The profile control effect had further improved.The gel has been applied on site in the E well group of Bohai X oilfield,with a maximum water content decrease of 5.2%,and a cumulative increase of 13786 m^(3) of oil.
关 键 词:水平注水井 双低乳液聚合物冻胶 调剖 性能评价 现场应用
分 类 号:TE39[石油与天然气工程—油气田开发工程]
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