控制力矩陀螺框架系统的谐振抑制与精度控制  被引量:10

Resonance elimination and precision control of CMG gimbal system

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作  者:徐向波[1] 房建成[1] 李海涛[1] 陈彦鹏[1] 

机构地区:[1]北京航空航天大学仪器科学与光电工程学院,北京100191

出  处:《光学精密工程》2012年第2期305-312,共8页Optics and Precision Engineering

基  金:国家973重点基础研究发展计划资助项目(No.2009CB724000);国家杰出青年科学基金资助项目(No.60825305)

摘  要:控制力矩陀螺(CMG)框架系统的速率控制精度是影响其输出力矩精度的重要因素,系统中谐波减速器提高了框架系统的动态响应能力,但其产生的机械谐振大幅降低了系统的控制精度。为抑制框架系统的谐振并满足系统的控制精度,本文建立了框架系统的动力学模型,根据系统动态性能要求选取合适的阻尼系数来设计系统主导极点,使控制器产生的零点与机械谐振对应的极点重合形成偶极子,从而抑制系统的机械谐振。仿真和实验结果显示:提出的方法有效地抑制了控制力矩陀螺框架系统的谐振,0.175rad/s恒速控制精度为0.002,0.175sin(2πt)rad/s正弦随动控制的幅值相对误差为3.28%,相位差为0.13rad。结果很好地满足了控制力矩陀螺的高精度输出力矩需求。The control precision of gimbal system for a Control Moment Gyro(CMG) is a main factor affecting the output torque accuracy of the CMG.Generally,a harmonic driver a harmonic driver is adopted to improve the dynamic response ability of the gimbal system,however,the induced mechanical resonance seriously reduces the control precision of the gimbal system.In order to eliminate the resonance and satisfy the control precision of the gimbal system,a kinetic model was set up.A proper damping ratio was chosen to design the dominating poles according to the demands of gimbal system for dynamic performance.The zeroes induced by a controller were calculated to be equal to the poles induced by mechanical resonance,so that the mechanical resonance was eliminated.Simulation and experiment results show that the proposed method eliminates the gimbal resonance of the CMG,and the control precision of 0.175 rad/s is 0.002.When the gimbal system tracks a 0.175 sin(2πt) rad/s sine given velocity,the relative amplitude error is 3.28% and the phase error is 0.13 rad.The control performance satisfies the demands of CMG for high output torque precision very well.

关 键 词:控制力矩陀螺 框架系统 谐振抑制 高精度控制 零极点配置 

分 类 号:V241.5[航空宇航科学与技术—飞行器设计]

 

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