中大型往复泵泵盖铸件的工艺设计及优化  

Design and Optimization of Casting Process for Medium and Large Reciprocating Pump Cover Casting

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作  者:孟伟娜 牛振华[1] 何雪 MENG Wei-na;NIU Zhen-hua;HE Xue(College of Mechanical Engineering,Anyang Vocational and Technical College,Anyang 455000,Henan,China;Engineering Training Centre,Guizhou Institute of Technology,Guiyang 550025,Guizhou,China)

机构地区:[1]安阳职业技术学院机电工程学院,河南安阳455000 [2]贵州理工学院工程训练中心,贵州贵阳550025

出  处:《铸造》2024年第1期114-120,共7页Foundry

基  金:2021年度河南省高等教育教学改革研究与实践重点项目(2021SJGLX708);2020年度安阳市科技发展计划项目。

摘  要:针对中大型往复泵泵盖铸件在生产过程中出现的缩松、缩孔等缺陷,利用AnyCasting铸造模拟软件对原工艺方案进行了凝固过程的模拟以及缺陷预测。结合缩孔缩松形成机理,分析了铸件产生缺陷的原因,并对原工艺方案进行了优化。采用优化后的原工艺方案能获得质量合格的铸件,但工艺出品率仅为45%。为获得质量合格的铸件,同时提高铸件工艺出品率,设计了新的工艺方案,通过对新工艺方案的模拟优化,铸件的工艺出品率提高到62%,达到了节能减材的目的,提高了企业的生产效益。In view of the defects such as shrinkage cavity and shrinkage porosity appeared in production process of Medium and Large pump cover casting,the solidification process and defects prediction were simulated of the original process scheme by using AnyCasting software.Combined with shrinkage cavity and porosity formation mechanism,the causes of defects in casting were analyzed,then the original process scheme was optimized.The casting with qualified quality can be obtained by using the optimized original process scheme,but the process yield was lower as 45%.In order to obtain qualified castings and improve the casting process yield,a new process plan was designed.Through the simulation and optimization of the new process plan,the casting process yield was increased to 62%,which achieved the purpose of energy saving and material reduction and improved the production efficiency of the enterprise.

关 键 词:泵盖铸件 工艺设计 工艺优化 工艺出品率 

分 类 号:TG245[金属学及工艺—铸造]

 

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